With a small lathe like most of us have, a push knurl is a terrible idea, and a pinch scissor knurl in its normal configuration has a one-to-two disadvantage in applying pressure making it hard to get sugfficient pressure to produce a good knurl.
After looking through various alternative designs, Paul & I decided to go ahead building a hydraulic knurling tool. Based on Paul’s initial design I went off and refined the details to come up with a specific plan and draw the CAD design (which I’ll eventually publish when I get it all finished).
After that, I figured I would start on the easy parts (the arms) and leave the rest to Paul ;-)
You can see some photos of the work here and here. The final result is:
Not too bad, although a little rought, and perhaps not quite as accurate as I might hope. Still, at the very least they should work as a proof of concept and hopefully will work adequately for the finished tool.
Saturday, October 27, 2007
Sunday, September 9, 2007
Shed Party
John and Peter came over for a bit of a roadtrip, we went to Jaydees and Hare and Forbes. John and Peter showing remarkable fiscal restraint.
Hey, it's only money right?
Pete's whole family is apparently crook, and he was under the weather by the time we got back from Hare and Forbes. John and I had to work hard to catch up, but we were soon there. As a result, productivity dwindled as the afternoon progressed but good fun was had. Mostly we spent our time, noses pressed against the polycarbonate, watching the NC router make a part for Peters dads drill press that John broke.
Hey, it's only money right?
Pete's whole family is apparently crook, and he was under the weather by the time we got back from Hare and Forbes. John and I had to work hard to catch up, but we were soon there. As a result, productivity dwindled as the afternoon progressed but good fun was had. Mostly we spent our time, noses pressed against the polycarbonate, watching the NC router make a part for Peters dads drill press that John broke.
Anodising sorted
The anodising tank has been playing up of late, At first I thought it was some dodgy metal that Keith gave me, but we had a bit of a shed party the other day and another job screwed up. I'd put some fresh acid in for it too. I spent nearly all of yesterday trying to figure the bloody thing out. Turns out that one of the electrode clips had corroded ALMOST to the point of being open circuit and was dropping enough voltage that the part was still anodising, but the current density was so low that no dye would stick to it. (Pore size is a function of current density).
It actually only took me an hour or so to figure this out, but murphy and a nasty hangover from the shed party ganged up on me and the fault was masked by a bunch of other things going wrong. Still, got there in the end. Apologies for those who've been waiting on jobs, I'm working through the backlog.
Monday, September 3, 2007
Router spindle speedup
For background, here's the CNC router I built. More here
The previous evolution of the spindle involved a timing belt drive, which worked OK, but was a bit inherently noisy and had (due to it being recycled) one pulley bore just a little off center. This resulted in some low (motor RPM) speed vibration that reverberated in the enclosure.
Since Keith did such a good job on the v-pulleys for the X2 conversion, I got him to make up a set for me. I made the decision to go for a bit more speed and changed the drive ratio from 2:1 to 3:1 while we were at it.
I haven't clocked it, but it should be doing something like 9KRPM now.
The improvement in noise was as expected. A little more high frequency noise, a lot less low frequency noise and about 50% louder when cutting metal. Happy with that.
The problem I had now though, was high frequency chatter. The finish on the part was terrible. At first I thought it might be the belt slipping, there isn't much wrap on that little pulley. I tweaked the mount to get some more serious tension but it didn't make a lot of difference. I concluded that the new speed must be exciting some resonant mode in my machine and made up the new spindle nose collar you see in the second pic. Always hated the little one I originally made; too thin and only two slots for the C spanner. The new one weighs about 4 times the old and has two more slots.
Anyhow, this made all the difference. Cuts at 50% more feed rate (600mm/min) now looked really nice. In fact I get reasonable cuts all the way up to 1000mm/min! The extra mass at that speed gyroscopically stabilises the spindle, compensating for the flimsy gantry, bonus!
PK
Tuesday, August 28, 2007
Vice Clamps
I managed to spend Friday on my lathe, but ended up spending most of the time making some mounting clamps for my vice. One the bright side, I got to use the new low profile clamps we made as a group project, and they worked brilliantly except that they slipped a little because the clamping force is so strong it pushed the clamps back. Paul assures me he had the same problem and resolved it by tightening the lock down screw more - I solved it by placing some other clamps directly behind the low profile clamps to make it impossible for the to slip backwards.
The end result looks good and should work nicely. I took them around to Paul's on the weekend and polished (I really don't have the patience for that!) and blackened them so I should get to try them later this week.
Saturday, August 25, 2007
Slotted pulleys
After dicking around with it in the lathe, I ended up making a fixture to hold the pulleys for the X2 Belt conversion in the mill vice. This worked out well as it allowed me to tune the widths of the slots by nudging the table left and right.. Need to make up a weener tool to do the small pulleys tomorrow.
PK
Friday, August 10, 2007
Elbow Part 2
I made it back to my lathe yesterday and did another part of my engine, the second part of an airway elbow. The collet chuck really is easy to use, although I am a bit concerned it may actually have a significant runout (0.16mm), which presumably comes from the spindle, and if so I have no idea how to adjust that.
Part 1 fits nicely in to the new part making a nice elbow - now I just have to figure out how to soft solder.
I think my confidence and ability is finally starting to pick up as I knock out these parts a little easier than before, although the more complicated and critical parts (like pistons and cylinders) still await!
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